Energy Efficiency Opportunities Public Report 2010-11

Part 1 - Corporation Details

Controlling Corporation                                                                                               Period to which this report relates

Insert the name of the Controlling Corporation exactly as it is registered with the EEO Program. The period to which the report relates is the total period of participation up to 30 June prior to when the report is due.

Queensland Nitrates Management Pty Ltd

From

1 July 2010

To

30 June 2011

Table 1.1 - Major Changes to Corporate Group Structure or Operations

Table 1.1 – Major Changes to Corporate Group Structure or Operations

None

 

 

Table 1.2 – Aggregate energy assessed covered in this report

Total energy use covered by all assessments in this report

3309733

GJ

Total energy assessed as percentage of total energy use of the corporate group*#

100

%

 
Declaration

Declaration of accuracy and compliance

The information included in this report has been reviewed and noted by the board of directors and is to the best of my knowledge, correct and in accordance with the Energy Efficiency Opportunities Act 2006 and Energy Efficiency Opportunities Regulations 2006.

 

Insert Name and Title of Signatory here

(Chair of the Board, CEO, or Managing Director)

Date


Part 2 - Assessment Outcomes

Table 2.1 – Assessment Details



Name of group member or business unit or key activity

Queensland Nitrates Pty Ltd

 

Total energy use in the last financial year

3309733

GJ

Energy use assessed in this entity as a percentage of total entity energy use*

100

%

Energy use assessed in this entity as a percentage of total corporate energy use

100

%

Accuracy of above estimates related to energy use assessed - only required if not ±5% or better

 

%

 

Period over which assessment was undertaken

 

1 July 2010

 

30 June 2011

Description of the way in which the entity carried out its assessment

 

Queensland Nitrate Pty Ltd (QNP) is a joint venture involving Dyno Nobel and CSBP (Wesfarmers). Dyno Nobel was acquired by Incitec Pivot Pty Ltd (IPL) in 2008. As its only operation, the Moura Ammonium Nitrate Plant accounts for 100% of the energy use of the company.

 

QNP has sought to meet the formal requirements of the Energy Efficiency Opportunities Regulations by preparing assessment reports for the site. In some cases assessments were initially completed to satisfy the EITE and NGERS programs. These assessments were modified where necessary to meet the intent and key requirements of EEO legislation. QNP has used qualified in house staff for the assessments, supplemented by advice from external corporate specialists.

 

 

Site-wide energy use (Natural Gas and Electricity) presented for this assessment period has been determined from commercial invoices and statements. Energy savings for individual opportunities have been calculated using internal mass balance techniques and process data system  (PI System). In this document QNP is reporting on 100% of the total energy to be assessed in the first EEO cycle.

*  Please note that, for individual sites that use more that 0.5PJ of energy, all energy use must be assessed (less a small proportion for non integral energy use).


Table 2.2 - Energy efficiency opportunities identified in the assessment

Table 2.2 – Energy efficiency opportunities identified in the assessment

Status of opportunities identified to an accuracy of better than or equal to ±30%

Total

Estimated energy savings per annum by payback period (GJ)

Total estimated energy savings per annum (GJ)

Number of opportunities

0 – < 2 years

2 – ≤ 4 years

> 4 years

 

No of Opps

GJ

No of Opps

GJ

No of Opps

GJ

Business

Implemented

2

1

80,522

1

20737

 

 

101,259

Response

Implementation Commenced

1

1

6378

 

 

 

 

6378

 

To be Implemented

1

1

6167

 

 

 

 

6167

 

Under Investigation

0

 

 

 

 

 

 

 

 

Not to be Implemented

0

 

 

 

 

 

 

 

 

Outcomes of assessment

Total Identified

4

2

93,067

1

20,737

 

 

113,804

Status of opportunities identified to an accuracy of worse than ±30%

Business

Implemented

0

 

 

 

 

 

 

 

Response

Implementation Commenced

0

 

 

 

 

 

 

 

 

To be Implemented

0

 

 

 

 

 

 

 

 

 

 

Under Investigation

3

1

32000

 

 

2

 

32,000

 

Not to be Implemented

10

1

4000

 

 

9

3000

7,000

Outcomes of assessment

Total Identified

13

 

 

 

 

13

 

39,000

Please note that Corporate Groups are not required to report opportunities with a payback greater than 4 years. Reporting this data is voluntary.

 

 

 

 


Table 2.3 - Details of significant opportunities identified in the assessment

Description of Opportunity

Voluntary Information

 Gas compositions around the ammonia synthesis loop are not adequately known. Better knowledge of the compositions can allow for fine tuning of the process, leading to improved conversion efficiency and reduced use of natural gas.

Business Response

Implementation Commenced

Energy saved (GJ)

6378

Greenhouse gas abated (CO2-e)

326 tonnes

$s saved

 

Payback period

1.4 years

 

 

Description of Opportunity

Voluntary Information

Automation of Nitric Acid Plant Start-ups can reduce the number of plant trips. The plant is at its maximum energy efficiency at design rates. Any period where a plant is in the process of ramping up to full rates is associated with lower energy efficiency, so any measure that reduces trips will reduce energy over a year. 

Business Response

To be implemented

Energy saved (GJ)

6167

Greenhouse gas abated (CO2-e)

1525 tonnes

$s saved

 

Payback period

3.3 years

 

 

Description of Opportunity

Voluntary Information

The Nitric Acid plant air filter was undersized, meaning that it was prone to blockage from airborne dust during adverse weather conditions, resulting in maintenance downtime with associated reduced energy efficiency.

The Air Filter was replaced with a larger unit. This has resulted in lower overall current draw and lower incidence of contamination of catalyst.

 

Business Response

Implemented

Energy saved (GJ)

80522

Greenhouse gas abated (CO2-e)

4723 tonnes

$s saved

 

Payback period

0.2 years